A Dutch friend of mine, Thijs Hessels, had improved the original cylinders by epoxying the outside curve, and giving the mixture a more upward direction. His private Aprilia proved faster than the 'works' bikes. The Aprilia racing boss, Jan Witteveen, demanded that Thijs should give those cylinders to him. Otherwise Thijs would not be able to get any more spare parts for his bike!!

Originally Posted by
jamathi
I started working with an existing engine, a ROTAX, with an existing cylinder and exhaust pipe.
During the year dozens of different exhaust pipes were tested.....
The original Rotax A duct was something like this....
With this modification a ROTAX cylinder gave 46,5HP instead of the normal 44.
This happened in 1994, a year later I started working for Aprilia.
They were still epoxying ROTAX cylinders, but had decided to make their own cylinder.
The development of this cylinder was to be my work.
This cylinder was called the APC, and was destined for all 125 and 250 private riders.
It gave the same 46,5HP, but of course without epoxy.
I got the oldest dyno there was, and had to learn to use the computerized system.
As I had never touched a computer before it was not so easy.
But I quickly learned, the system was very precise and repeatable.
I was given the casting models and had to go to the foundry to have some cylinders cast,
While waiting for the castings to be machined I worked with ROTAX cylinders.
I won some power by making the auxiliary ports bigger, but they were already too high I thought.
So I made sure the APC cylinders had lower auxiliary ports, and I also filed their sand cores to make the exhaust duct a lot smaller, as I had already, successfully, tried on some ROTAX cylinders.
There were some small mistakes in the casting models, they were quickly corrected.
And then real development could begin!
I started by making the B-ports and ducts as wide as I could, and this improved bottom power, without losing at the top.
And I had one casting with a narrower C-port, made by filing the sand core.
Here the B-ports could still be made wider, and it proved to be the best cylinder of the lot.
So we got to 48HP
We also bought a lot of dentist tools and burrs, and a filing machine.
And a flow bench.
Power improved by making the auxiliary ducts longer, and wider.
But at a certain point we made a hole, ending up in the cooling water space!!!!
To cure this the casting model had to be modified.
I also had a wooden model made for use on the flow bench.
To determine the best size of the auxiliary ports and ducts.
They seemed to 'like' having a downward angle.
The casting model was modified in this way, and so we reached 49HP.
I decided to try to make the exit of the exhaust duct, and the flange, a bit wider, and won another 0,6HP
Bookmarks