Kel sent me this ......
jan thiel on part throttle deto
"I am 100% convinced our engine could have run for 6 hours at max power without seizing.
The problems arise when you close the throttle, or run part throttle!
The piston is mainly cooled by the transfer flow.
And at part throttle there is less transfer flow, causing detonation (auto ignition)
The entering fresh charge is ignited by the remaining, hot, burned gases!
You can see very severe damage to the piston after maybe 10 seconds at 20% throttle.
This still is an unresolved problem! I was thinking about a way to  reduce engine power without closing the throttle. But how can you do  this? I did not find a solution before I retired.
And nobody else was really interested.
At 100% throttle the engine was undestructible!
By making the transfer ports as wide as possible we had very good piston cooling."
No answer here but at least we are not alone with engines that fail on part throttle
I scraped the full coversation below from here:- 
http://www.pit-lane.biz/t3173p60-gp1...vermars-part-2
Brian Callahan
Jan or others, how did you control the tuned pipe wall temperature (or  EGT directly?) when testing on dyno? This seemed the most difficult  thing to mimic when testing either the GP engines at QUB or my R/C boat  engines, in the lab. The inertial dyno or computer controlled brake seem  to work best because we can match the test engine's acceleration with  reality. On steady-state testing, EGT would simply climb 500, 600, 700,  750 °C until way past reality and the piston would seize.
Frits Overmars
This has always been one of Jan's greatest handicaps. He has asked for  an inertial test bench over and over, but Aprilias race director  Witteveen, or The Great Leader as we call him, never deemed it  necessary....
Jan Thiel
When EGT goes up and up there should be some serious problem with the engine.
We never had pistons seize during our steady state tests.
Working on the dyno continuously 5 days a week!
I am 100% convinced our engine could have run for 6 hours at max power without seizing.
The problems arise when you close the throttle, or run part throttle!
The piston is mainly cooled by the transfer flow.
And at part throttle there is less transfer flow, causing detonation (auto ignition)
The entering fresh charge is ignited by the remaining, hot, burned gases!
You can see very severe damage to the piston after maybe 10 seconds at 20% throttle.
This still is an unresolved problem! I was thinking about a way to  reduce engine power without closing the throttle. But how can you do  this? I did not find a solution before I retired.
And nobody else was really interested.
At 100% throttle the engine was undestructible!
By making the transfer ports as wide as possible we had very good piston cooling.
As Frits has written, I would have liked to have also a dynamic testing possibility, with a flywheel.
In my opinion you should simulate a straight, starting at around 10.000 rpm, and shift through the gears
until you reach top speed. And with the airbox as used on the bike, with a ventilator that simulates the raising
air speed as it would be on track! Maybe it is interesting to know that without a ventilator the engine gave
less power with the airbox fitted.
I was told that such a testing system was too expensive.
And unnecessary as we won anyway!
I can also see a disadvantage of 'dynamic' testing.
Because the duration of the test is so short you can get away with very extreme (too extreme?) settings,
without damage.
GrahamB
Remember that retarding the ignition is used at high rpm to increase  exhaust temps and effectively shorten the pipe. So it's likely to  increase the heating of the front edge of the piston...
Haufen
Yes I know, but part load egt is usually lower than full load egt. And I  think most of us would prefer higher part load egt over part load  detonation. Of course, how far one could go and how far one would need  to go would have to be tested, and how much would be needed would depend  on the engine.
Mic
How about much larger travel on the exhaust power valve.
With a shorter exhaust port duration power is lower. And this is already controlled with the stepmotor over the ECU.
Jan Thiel
This causes detonation (auto ignition)
The problem is that the burned gases do not exit the cilinder!
Retarding ignition also does not make sense.
As you have an AUTO-inition problem!
So the engine does not 'listen' to its ECU anymore!
What you would need is the same fresh gas flow, but with less HP!
Not easy to achieve!
A variable tailpipe might help.
Jan Thiel
Haufen, We also had such a test bench at Aprlia.
The prototype of this test bench was developed by Apicom in collaboration wit Aprilia.
So we had it first, and now anyone can buy it.
It was helpful but not what I wanted.
A so-called step test.
And without the airbox!
Frits Overmars
Like Jan wrote, a shorter exhaust duration will worsen the detonation. What happens is this:
During normal operation, the blowdown time.area of the exhaust ports is  sufficient to drop the cylinder pressure below the crankcase pressure  before the transfer ports open, even at high rpm.
At part-throttle that cylinder pressure will drop to the same level, but  now the crankcase pressure is much lower and exhaust gases will enter  the transfer ducts, contaminating and heating the fresh mixture even  before it enters the cylinder.
A theoretical solution would be a power valve that enlarges the normal  exhaust timing instead of lowering it. But that is impractical as it  would ruin the shape of the exhaust duct and it would cause cooling  problems in the cylinder's exhaust area.
A variable tailpipe area, like Jan says, can be a more practical  approach. I designed a simple solution, shown in the drawing below, but  then two-stroke development at Aprilia was terminated because of Dorna's  ban on two-strokes
Howard Gifford
Another way to lower HP without sacrificing piston cooling would be to  richen the mixture when you want to lower the power. With a signal to a  fuel enrichening solenoid you could achieve a power range. It would then  be instantaneous and programmable. Not enviornmentally friendly but  would work for racing. The mixture ratio difference from high power to  low power would need to be just rich enough before a misfire and just  lean enough for sustained high power.
The variable tailpipe idea will work but I suspect the pipe temperature  would drop off and it would take several seconds to regain full power.  But then again rich mixture may have the same problem.
Two strokes are like redheads. Hard to figure out and very temperamental. But when they are happy they are a lot of fun!
HG
Jan Thiel a écrit:
The entering fresh charge is ignited by the remaining, hot, burned gases!
You can see very severe damage to the piston after maybe 10 seconds at 20% throttle.
This still is an unresolved problem! I was thinking about a way to  reduce engine power without closing the throttle. But how can you do  this? I did not find a solution before I retired.
And nobody else was really interested.
Institute of TwoStrokes
On aftermarket ignitions I use there is a mode I can switch on where a  number of indivdual sparks are cut, depending on throttle position. It  is now only configured for cutting 1 in every 3 sparks on over run(tps  <10% with high rpm). Would that sort of system solve the part  throttle detonation? If the number of sparks cut could be varied along  with TPS for this to begin and end? If it would be helpful I'm certain  the manufacturer would only need a software change to do this.
Jan Thiel
I certainly thought about cutting sparks.
But remember: the problem was AUTO-ignition!
GrahamB a écrit:
Remember that retarding the ignition is used at high rpm to increase  exhaust temps and effectively shorten the pipe. So it's likely to  increase the heating of the front edge of the piston...
Jan Thiel
Indeed, retarding too much caused detonation!
Institute of TwoStrokes a écrit:
Jan Thiel a écrit: The entering fresh charge is ignited by the  remaining, hot, burned gases! You can see very severe damage to the  piston after maybe 10 seconds at 20% throttle.
This still is an unresolved problem! I was thinking about a way to  reduce engine power without closing the throttle. But how can you do  this? On aftermarket ignitions I use there is a mode I can switch on  where a number of individual sparks are cut, depending on throttle  position. Would that sort of system solve the part throttle detonation?
Frits Overmars
As Jan pointed out, once you have auto-ignition, the engine does not  listen to its ECU any more. So you would have to start skipping sparks  well before the onset of detonation.
In a foul-stroke your proposed system does work, but a two-stroke would  react far from linear. For example, if you skip 1 in 4 sparks, you will  loose much more than 25% of engine power because that one missing spark  will cause the gasdynamics processes to collapse. The main problem would  be to realise a smooth transition from intermittent to full ignition.
Jan Thiel a écrit:
Retarding ignition also does not make sense.
As you have an AUTO-inition problem!
So the engine does not 'listen' to its ECU anymore!
What you would need is the same fresh gas flow, but with less HP!
Not easy to achieve!
A variable tailpipe might help.
Haufen
I think I expressed myself unclearly. What I meant was the following:
Imagine your engine with the throttle opened just above the  auto-ignition range. Then you have sufficient transfer flow, but too  much power. To lower the power, now retard the ignition. Then you still  have sufficient transfer flow, but with less power.
I think Honda used auto-ignition to their advantage on two-strokes. As  far as I remember they did it with a (very) variable exhaust power  valve.
Frits Overmars a écrit:
Mic a écrit:
How about much larger travel on the exhaust power valve. With a shorter  exhaust port duration power is lower. And this is already controlled  with the stepmotor over the ECU.
Frits Overmars a écrit:
Like Jan wrote, a shorter exhaust duration will worsen the detonation. What happens is this:
During normal operation, the blowdown time.area of the exhaust ports is  sufficient to drop the cylinder pressure below the crankcase pressure  before the transfer ports open, even at high rpm.
At part-throttle that cylinder pressure will drop to the same level, but  now the crankcase pressure is much lower and exhaust gases will enter  the transfer ducts, contaminating and heating the fresh mixture even  before it enters the cylinder.
A theoretical solution would be a power valve that enlarges the normal  exhaust timing instead of lowering it. But that is impractical as it  would ruin the shape of the exhaust duct and it would cause cooling  problems in the cylinder's exhaust area.
A variable tailpipe area, like Jan says, can be a more practical  approach. I designed a simple solution, shown in the drawing below.
Attachment 269228
Haufen
I think I have not gotten behind the variable tailpipe idea, yet. What  would you like to vary with it and to achieve which effects? At little  throttle openings the pressure inside the exhaust pipe is already very  close to atmospheric pressure (if not even) on most engines. And if you  had say 100mbar inside the pipe at the critical throttle opening, then  the engine might have had more power with a bigger tailpipe.
Attachment 269228
Frits Overmars
'Opening' the end of the reflector will cause a substantial weakening of  the reflected pulse and thus less charging of the cylinder. Izze  simple, no?
Haufen a écrit:
Variable transfer timing would be nice also, if feasible.
Frits Overmars
That would be my ideal. Lowering all the transfer roofs would shorten  the transfer timing and lengthen the blowdown timing, so the cylinder  pressure would drop further before the transfers would open. It would  cure the hig revs/low power-detonation and it would improve the power  band because a too early-returning exhaust pulse would have less  opportunity to push the fresh cylinder contents back into the crankcase.
A controllable transfer height would even make a throttle valve unnecessary.
There's only the little problem of how to build it...
Jan Thiel
Haufen, Auto-ignition usually occurs between 10 to 40% throttle at high revs.
In fast, non full throttle corners.
Retarding the ignition was tried to diminish power.
This makes the exhaust very hot.
Then, when you need full power, it is not there because the exhaust temperatures are wrong.
This takes a little time, when the engine is back to full power you are already at the end of the straight!
The same goes for water injection in the exhaust.
It was tried by Rotax about 25 years ago.
There was a LOT more power at low revs, so the rider had to take it easy when opening the throttle.
But the engine revved a little bit less, because the exhaust temperature did not recover at high revs.
And lap times became actually slower.
After a day of testing the system was switched off.
Lap times immediately improved!
A very important thing when accelerating is the power you have after changing gear.
Spark interruption may be not so good for this!
As I did not have the dyno I wanted this gearchange effect could not be tried on the dyno, very regrettably!
Retarding the ignition and weakening the mixture by powerjet can also have a negative effect on this.
The exhaust temperature should be 'Right' for the No. of revs after you change gear.
If the temperature is too high there will be less power!
So it is REALLY complicated!
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