Yeah, I've been there a few times now. Last time was today, reading about disconnecting the intake flapper. Someone had already done it.
Also checked the air filter and, while at it, found the airbox-to-throttle ducts were not properly tightened. Probably the work (unwork?, malwork?, beerwork?) of whoever did the flapper mod. That reminded me I need a new set of ball-end hex keys. The filter didn't look too bad and it's only done 20,000 (recco change of air filter is 40,000!!!) so I'll leave that for the time being.
Nicked down to the local Yam shop on the Suzi FXFXFXF'er and got some fresh compression nuts for the screen etc. too.
Ticks over and runs nicely but I suspect it could do with a slight balance tweak on the throttles. No hurry on that.
Beer o'clock here. Cheers

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